OPERATIONS
8 plugs were set.
Due to the large ID of the dissolvable frac plug, the customer was able to successfully flow back the wellbore and start production while the frac plugs were dissolving.
20 days later, fine returns confirmed that all 8 plugs were fully dissolved.
WELL PROFILE
Oil Well
MD 9,442Ft TVD 5,344Ft
2,641 Ft Hor. Interval 5-1/2” 23# Csg.
DHT 98°F
Formation Fluid CL- <500mg/l
CHALLENGES
Low BHT
Low Chlorine Content
SOLUTIONS
Special Dissolving materials with self-heating features
Slim size single slip design shorten dissolution time
RESULTS
Plug set and ball seated with no issues
Pressure held up when fracturing Immediate flowback after frac.
Full Dissolution confirmed by fine returns in flowback 20 days later